LAPSE:2024.0396
Published Article

LAPSE:2024.0396
Heat Transfer and Thermal Efficiency in Oxy-Fuel Retrofit of 0.5 MW Fire Tube Gas Boiler
June 5, 2024
Abstract
Industrial boilers cause significant energy wastage that could be mitigated with oxy-fuel combustion versus traditional air combustion. Despite several feasibility studies on oxy-fuel burners, they are widely avoided in industry due to major infrastructural challenges. This study measured the performance and heat transfer characteristics of each component in a 0.5 MW fire tube gas boiler after retrofitting it with an oxy-fuel burner. Comparisons were drawn across three combustion modes—air combustion, oxy-fuel combustion, and oxy-fuel flue gas recirculation (FGR). The Dittus−Boelter equation was employed to predict heat transfer in the fire tube for all combustion modes at full load (100%). Heat transfer in the latent heat section of the economizer was measured and compared with predictions using the Zukauskas equation. With this retrofit, oxy-fuel combustion improved the thermal efficiency by about 3−4%. In oxy-fuel combustion, the flow rate of exhaust gas decreased. When integrated into an existing fire tube boiler, the fire tube’s heat transfer contribution diminished greatly, suggesting the economic viability of a redesigned, reduced fire tube section. Additionally, a new design could address the notable increase in gas radiation from the fire tube in oxy-fuel and FGR, as well as aid in the efficient recovery of condensation heat from exhaust gases.
Industrial boilers cause significant energy wastage that could be mitigated with oxy-fuel combustion versus traditional air combustion. Despite several feasibility studies on oxy-fuel burners, they are widely avoided in industry due to major infrastructural challenges. This study measured the performance and heat transfer characteristics of each component in a 0.5 MW fire tube gas boiler after retrofitting it with an oxy-fuel burner. Comparisons were drawn across three combustion modes—air combustion, oxy-fuel combustion, and oxy-fuel flue gas recirculation (FGR). The Dittus−Boelter equation was employed to predict heat transfer in the fire tube for all combustion modes at full load (100%). Heat transfer in the latent heat section of the economizer was measured and compared with predictions using the Zukauskas equation. With this retrofit, oxy-fuel combustion improved the thermal efficiency by about 3−4%. In oxy-fuel combustion, the flow rate of exhaust gas decreased. When integrated into an existing fire tube boiler, the fire tube’s heat transfer contribution diminished greatly, suggesting the economic viability of a redesigned, reduced fire tube section. Additionally, a new design could address the notable increase in gas radiation from the fire tube in oxy-fuel and FGR, as well as aid in the efficient recovery of condensation heat from exhaust gases.
Record ID
Keywords
economizer, fire tube boiler, heat transfer, oxy-fuel combustion, retrofit
Subject
Suggested Citation
Ahn J. Heat Transfer and Thermal Efficiency in Oxy-Fuel Retrofit of 0.5 MW Fire Tube Gas Boiler. (2024). LAPSE:2024.0396
Author Affiliations
Ahn J: School of Mechanical Engineering, Kookmin University, Seoul 02707, Republic of Korea [ORCID]
Journal Name
Processes
Volume
12
Issue
5
First Page
959
Year
2024
Publication Date
2024-05-09
ISSN
2227-9717
Version Comments
Original Submission
Other Meta
PII: pr12050959, Publication Type: Journal Article
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LAPSE:2024.0396
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https://doi.org/10.3390/pr12050959
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Jun 5, 2024
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Jun 5, 2024
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