LAPSE:2023.7112
Published Article
LAPSE:2023.7112
Research on the Modification of Coal Adaptability and Carbon Emissions Reduction Technology for Coal-Fired Boilers
Dan Peng, Ben Wang, Xingfei Cai, Lei Bei
February 24, 2023
In order to solve the problems of the high temperature of flue gas, low boiler efficiency, and the high concentration of nitrogen oxide (NOx) emissions for a 330 MW boiler fired with lean coal in a power plant, an adaptation modification by using different type of coals in the power generation unit (including pulverizing system, burners, heating surface, and so on) was carried out. The performances of boilers were tested under different combustion conditions before and after the modification. The results of the test show that the volatile content is higher and easy to burn out, and the combustible content of fly ash and slag are greatly reduced after the change in coal type (while lean coal is changed into bituminous coal). At the same time, the low-temperature economizer can greatly reduce the flue gas temperature, thus increasing the efficiency from 90.36% (lean coal, corrected) to 92.71% (bituminous coal). After the change in coal type (lean coal to bituminous coal) and the shift to low-nitrogen combustion (using low-nitrogen burner and OFA technology), the flame temperature in the main combustion area of the boiler decreases, the thermal-type NOx is reduced, and the volatile content of bituminous coal is higher in the anoxic atmosphere of the main combustion zone where the excess air coefficient is small. The intermediate reductive products tend to produce more, which can restrain and reduce NOx. Therefore, the concentration of NOx emissions can be greatly reduced. NOx average emissions at the economizer outlet decreased by 68%, from 864 mg/Nm3 to 279.4 mg/Nm3. A low-temperature economizer uses waste heat to heat feed water, which reduces coal consumption by about 1.32 g/(kW·h). The coal consumption for power supply after modification is reduced by 9.83 g/(kW·h) and the annual energy saving is 16,776 tons of standard coal, while the total carbon dioxide emissions reduction is 41,213.60 tons after the unit modification.
Keywords
boiler performance, carbon emission reduction technology, coal adaptability, comprehensive modification, NOx, pulverizing system
Suggested Citation
Peng D, Wang B, Cai X, Bei L. Research on the Modification of Coal Adaptability and Carbon Emissions Reduction Technology for Coal-Fired Boilers. (2023). LAPSE:2023.7112
Author Affiliations
Peng D: Henan Engineering Technology Research Center for Energy Conversation and Environmental Protection in Power Plant, Zhengzhou Electric Power College, Zhengzhou 450000, China
Wang B: State Key Laboratory of Coal Combustion, Huazhong University of Science and Technology, Wuhan 430074, China
Cai X: Shenzhen Zhongyuan Environmental Technology Co., Ltd., Shenzhen 518054, China
Bei L: State Key Laboratory of Coal Combustion, Huazhong University of Science and Technology, Wuhan 430074, China
Journal Name
Energies
Volume
15
Issue
24
First Page
9533
Year
2022
Publication Date
2022-12-15
Published Version
ISSN
1996-1073
Version Comments
Original Submission
Other Meta
PII: en15249533, Publication Type: Journal Article
Record Map
Published Article

LAPSE:2023.7112
This Record
External Link

doi:10.3390/en15249533
Publisher Version
Download
Files
[Download 1v1.pdf] (1.2 MB)
Feb 24, 2023
Main Article
License
CC BY 4.0
Meta
Record Statistics
Record Views
54
Version History
[v1] (Original Submission)
Feb 24, 2023
 
Verified by curator on
Feb 24, 2023
This Version Number
v1
Citations
Most Recent
This Version
URL Here
https://psecommunity.org/LAPSE:2023.7112
 
Original Submitter
Auto Uploader for LAPSE
Links to Related Works
Directly Related to This Work
Publisher Version