LAPSE:2023.13632
Published Article

LAPSE:2023.13632
Pressure Drop Optimization of the Main Steam and Reheat Steam System of a 1000 MW Secondary Reheat Unit
March 1, 2023
Abstract
The pressure drop of a main steam and reheat steam system should be optimized during the design and operation of a thermal power plant to minimize operation costs. In this study, the pressure drop of the main steam pipe and reheat steam pipe of a 1000 MW secondary reheat unit are optimized by modulating the operation parameters and the cost of operation is explored. Optimal pipe specifications were achieved by selecting a bend pipe and optimizing the pipe specifications. The pressure loss of the main steam pipeline was optimized to 2.61% compared with the conventional pressure drop (5%), the heat consumption of steam turbine was reduced by about 0.63 kJ/(kW·h), the standard coal consumption was minimized by about 0.024 g/(kW·h), and the total income in 20 years is approximated to be CNY 217,700. The primary reheat system was optimized to 4.88%, the steam turbine heat consumption was reduced by about 7.13 kJ/(kW·h), the standard coal consumption decreased by about 0.276 g/(kW·h), and the total income in 20 years is projected to be CNY 20.872 million after the optimization of the pressure drop. The secondary reheat system was optimized to 8.13%, the steam turbine heat consumption was reduced by about 7.86 kJ/(kW·h), the standard coal consumption decreased by about 0.304 g/(kW·h), and the total income in 20 years is projected to be CNY 22.7232 million after the optimization of the pressure drop. The research results of the present study provide a guide for the design and operation of secondary reheat units to achieve an effective operation and minimize costs.
The pressure drop of a main steam and reheat steam system should be optimized during the design and operation of a thermal power plant to minimize operation costs. In this study, the pressure drop of the main steam pipe and reheat steam pipe of a 1000 MW secondary reheat unit are optimized by modulating the operation parameters and the cost of operation is explored. Optimal pipe specifications were achieved by selecting a bend pipe and optimizing the pipe specifications. The pressure loss of the main steam pipeline was optimized to 2.61% compared with the conventional pressure drop (5%), the heat consumption of steam turbine was reduced by about 0.63 kJ/(kW·h), the standard coal consumption was minimized by about 0.024 g/(kW·h), and the total income in 20 years is approximated to be CNY 217,700. The primary reheat system was optimized to 4.88%, the steam turbine heat consumption was reduced by about 7.13 kJ/(kW·h), the standard coal consumption decreased by about 0.276 g/(kW·h), and the total income in 20 years is projected to be CNY 20.872 million after the optimization of the pressure drop. The secondary reheat system was optimized to 8.13%, the steam turbine heat consumption was reduced by about 7.86 kJ/(kW·h), the standard coal consumption decreased by about 0.304 g/(kW·h), and the total income in 20 years is projected to be CNY 22.7232 million after the optimization of the pressure drop. The research results of the present study provide a guide for the design and operation of secondary reheat units to achieve an effective operation and minimize costs.
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Keywords
1000 MW secondary reheat unit, main steam and reheat steam system, pressure drop optimization
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Suggested Citation
Li Y, Liu J, Huang G. Pressure Drop Optimization of the Main Steam and Reheat Steam System of a 1000 MW Secondary Reheat Unit. (2023). LAPSE:2023.13632
Author Affiliations
Li Y: MOE Key Laboratory of Regional Energy and Environmental Systems Optimization, College of Environmental Science and Engineering, North China Electric Power University, Beijing 102206, China; State Key Joint Laboratory of Environmental Simulation and Pollut [ORCID]
Liu J: Shandong Electric Power Engineering Consulting Institute Corp., Ltd., Jinan 250013, China
Huang G: MOE Key Laboratory of Regional Energy and Environmental Systems Optimization, College of Environmental Science and Engineering, North China Electric Power University, Beijing 102206, China
Liu J: Shandong Electric Power Engineering Consulting Institute Corp., Ltd., Jinan 250013, China
Huang G: MOE Key Laboratory of Regional Energy and Environmental Systems Optimization, College of Environmental Science and Engineering, North China Electric Power University, Beijing 102206, China
Journal Name
Energies
Volume
15
Issue
9
First Page
3279
Year
2022
Publication Date
2022-04-29
ISSN
1996-1073
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PII: en15093279, Publication Type: Journal Article
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LAPSE:2023.13632
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https://doi.org/10.3390/en15093279
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